Register now to get rid of these ads!

Technical The Geoffrey Skene 1932 Roadster

Discussion in 'Traditional Hot Rods' started by Dennis Lacy, Jul 9, 2023.

  1. Tim
    Joined: Mar 2, 2001
    Posts: 18,205

    Tim
    Member
    from KCMO

    Looks great so far, I’m mostly impressed you busted all those rivets out so nice and in short time to boot
     
    JalopyJimbo and Dennis Lacy like this.
  2. subscribe!!!!
     
    Dennis Lacy likes this.
  3. x77matt
    Joined: Mar 2, 2004
    Posts: 828

    x77matt
    ALLIANCE MEMBER

    This will be awesome! Looking forward to the journey
     
    Dennis Lacy likes this.
  4. sshep
    Joined: Oct 13, 2018
    Posts: 281

    sshep
    ALLIANCE MEMBER

    X2
     
    Dennis Lacy likes this.
  5. Agreed. I've been following this build on IG, but it's so nice to have the in-depth detail that this thread will (and has already) provide.
     
    Kelly Burns and Dennis Lacy like this.
  6. Subscribed!
     
    Dennis Lacy likes this.
  7. Dennis Lacy
    Joined: Apr 27, 2008
    Posts: 1,407

    Dennis Lacy
    Member

    PART 4

    With the frame secured to the fixture I sent it and the X-member pieces out for media blasting. Shout out to Azusa Refinishing in Azusa, California. They handle all of our media blasting and powder coating needs.

    IMG_7390.jpeg

    IMG_7391.jpeg

    Once the frame was blasted some problem areas were revealed. The area where the steering gears mounts was a total mess. I didn’t get any pictures of what was there, unfortunately, but the previous person had built this box section out of 1/4” plate and had it bolted into the frame rail. The box had brackets welded to it to mount a Speedway reverse-Corvair steering box, more typically used for kit T-Buckets and other smaller hot rods. The steering shaft poked through the frame crooked. Total POS. That left behind a bunch of extra holes and they had put some kind of a ring in the big center hole. Three holes had been brazed closed so I had to drill those out larger to be sure any trace of the brass was gone. I also had to drill out the other two poorly filled holes as they were full of contamination voids. I made a handful of plugs and a disc to fill the big hole, welded it all up and metal finished as it was better to just start over.

    IMG_7396.jpeg

    I failed to document the process as I just got going and was in the zone but here it is the finished result. Note the red lines drawn on the top of the rail. Those are to show a wedge shaped piece that had been cut out as well to clear the stupid Corvair box. Now I have a clean slate to put the holes back to original.

    IMG_7708.jpeg

    The other areas of damage are on both frame rails right behind the front cross member. It looks like they were attempting to fill the original shock holes and another pair of holes and it all went to hell. They had actually drilled tiny holes at the ends of a lot of the cracks. What a mess!

    IMG_7395.jpeg

    IMG_7394.jpeg

    The best way to fix this was just to cut the whole bad area out. The area was marked, cut out and patch plates made. I also made plugs to fill what were probably supposed to be be holes for the front brake hoses. Now it’s like it never happened.

    IMG_7799.jpeg

    IMG_7804.jpeg

    IMG_7809.jpeg
     
    Last edited: Jul 16, 2023
  8. Dennis Lacy
    Joined: Apr 27, 2008
    Posts: 1,407

    Dennis Lacy
    Member

    PART 5

    With the frame rail damage repaired I turned my attention the X-member. The first step was to get the 3 pieces bolted together to check fit and alignment. Who ever had taken that old frame apart in the past wasn’t very graceful and bent the crap out of the lower X flanges where they are supposed to fit up to the center saddle.

    IMG_8122.jpeg

    IMG_8123.jpeg

    I hammered the flanges into general position and then used some heat to perfectly form the flanges to the saddle.

    IMG_8124.jpeg

    IMG_8126.jpeg

    With the flanges fixed the remainder of the holes were lined up and bolted. Then, after a little twisting and tweaking I had the X sitting even and square.

    IMG_8127.jpeg

    IMG_8128.jpeg

    IMG_8129.jpeg

    IMG_8130.jpeg

    IMG_8131.jpeg

    The X-member was then laid on top of the frame for a look and to start planning my attack.

    IMG_8132.jpeg

    IMG_8133.jpeg

    IMG_8134.jpeg
     
  9. Dennis Lacy
    Joined: Apr 27, 2008
    Posts: 1,407

    Dennis Lacy
    Member

    PART 6

    Aside from the X-member being a superior design for frame strength and rigidity, the biggest motivation to ditching the original K-member is the transmission shown below. It is a 1950’s French built Pont A Mousson. It is an aluminum, fully synchronized wide ratio unit that bolts directly to a Ford Flathead and was used in the French Ford Comete. A pretty rare find here in the States! The 1933/1934 X-member was chosen particularly because of the wider span between the two sides vs. later 30’s X-members which are significantly closer together at the center. Geoff acquired this rare trans some years ago and had it completely gone through by Jody’s Transmissions.

    For more details I found a HAMB thread with good information on these here:

    https://www.jalopyjournal.com/forum/threads/flathead-ford-tranny-what-is-it-from.344883/

    IMG_0601.jpeg

    So obviously this big trans isn’t going to fit the stock 33/34 X-member saddle either, but I can fix that! After careful measuring and calculating I drew out the cut lines on the saddle (followed by a revision) and then took my time carving it out. TIP: Always save your worn down cut-off discs because they can be used to more precisely cut along a radius where a new or less worn disc would be too big to follow the line.

    IMG_8305.jpeg

    IMG_8306.jpeg

    IMG_8307.jpeg

    Then I realized I needed a way to roll the filler plates. I recalled friend and fellow builder Derek Bower years ago describing to me how he rolled a hood top for his roadster. I clamped a scrap of large pipe to the edge of my welding table with spacers underneath that would let the material just barely slide under the pipe. I did one practice piece successfully so I moved on to the actual parts.

    IMG_8311.jpeg

    I’m using 3/16” thick cold roll and decided to make life easier by making the filler in 2 halves rather than attempt a single continuous piece. I’m either good or got lucky and made both sides on the first try. I left the material longer than needed to have leverage while bending then trimmed the excess off. IMG_8314.jpeg

    IMG_8315.jpeg

    The upper corners were then trimmed to fit so the plates would sit flush. I wanted to retain the original nut plate that mounts the 33/34 E-brake handle so a notch was needed to clear it.

    IMG_8548.jpeg

    IMG_8549.jpeg

    IMG_8550.jpeg

    Then I decided it might be advantageous to be able to use the two remaining holes on the back side of the saddle where the original mechanical brake lever shaft used to go but the nut plates went away with the part I cut out so I made a pair of 3/8” thick threaded blocks to fit inside the holes. I don’t know what they will be used for yet, if anything, but it’s nice to have options.

    IMG_8552.jpeg

    IMG_8554.jpeg

    IMG_8632.jpeg
     
    Last edited: Jul 16, 2023
  10. Tow Truck Tom
    Joined: Jul 3, 2018
    Posts: 2,586

    Tow Truck Tom
    Member
    from Clayton DE

    Love that crack'g substitute fix.
    It is apparent,,,,, You will make the right choices
    Restore and rebuild a winner
     
    Dennis Lacy likes this.
  11. Dennis Lacy
    Joined: Apr 27, 2008
    Posts: 1,407

    Dennis Lacy
    Member

    PART 7

    With the threaded blocks installed it was time to fully weld the plates but they weren’t a perfect match to radius’ cut in the saddle so I blue’d the areas, scribed using the plates as a guide and trimmed the saddle exactly. Here’s one of the 4 radius’ as an example.

    IMG_8625.jpeg

    IMG_8627.jpeg

    The plates were position and welded in the corners. They came up a little short of joining in the middle so a filler strip was added because with how good they fit otherwise I wasn’t about to start over!

    IMG_8633.jpeg

    IMG_8634.jpeg

    IMG_8635.jpeg

    IMG_8639.jpeg

    With that I finished welding and then metal finished.

    IMG_8740.jpeg

    IMG_8741.jpeg

    IMG_8745.jpeg

    IMG_8744.jpeg

    Ta Da!

    IMG_8748.jpeg

    I finished up by media blasting the saddle and bolting the X-member back together. Not too shabby!

    IMG_8851.jpeg

    IMG_8855.jpeg
     
    Last edited: Jul 16, 2023
  12. Outback
    Joined: Mar 4, 2005
    Posts: 2,817

    Outback
    Member
    from NE Vic

    Looking good. That gearbox is a cool thing, worth the effort!
    The drillings on the cracks are to stop the crack from spreading - an aviation technique - it seems they didn't get the end of the crack - as it has cracked beyond the 'stop drill hole' & besides you can weld steel, so don't know why they didn't do that!???
     
    Last edited: Jul 16, 2023
    RICH B and Dennis Lacy like this.
  13. krylon32
    Joined: Jan 29, 2006
    Posts: 9,871

    krylon32
    ALLIANCE MEMBER
    from Nebraska
    1. Central Nebraska H.A.M.B.

    Following this thread and it's very informational as usual. Interesting I did a 33/34 chassis for a customer that wanted to keep the wishbone stock and run a T5 trans. I did virtually the identical fix to the center support, I got lucky and had the local welding shop roll a filler piece that fit with it being one piece. Worked great. I like everything about this project.
     
  14. Bugguts
    Joined: Aug 13, 2011
    Posts: 935

    Bugguts
    Member

    Very cool build so far. I’m looking forward to seeing more! Subscribed
     
    continentaljohn and Dennis Lacy like this.
  15. Tim
    Joined: Mar 2, 2001
    Posts: 18,205

    Tim
    Member
    from KCMO

    Turned out slick
     
    Dennis Lacy likes this.
  16. What a great build thread! Thanks for the informative information.
     
    Dennis Lacy likes this.
  17. Dennis Lacy
    Joined: Apr 27, 2008
    Posts: 1,407

    Dennis Lacy
    Member

    It’s definitely odd. I understand drilling holes to head off a crack but like you I don’t understand why they would waste the time to do that in this case? No matter now, I took care of that!

    Thank you! I’ve seen the saddle mod done quite a few times but had never seen the process. So I cut the middle out and then said “Now what?” The clamped pipe actually worked really well but it took some muscle. Glad it didn’t have to be 1/4”!
     
  18. 282doorUK
    Joined: Mar 6, 2015
    Posts: 473

    282doorUK

    Great thread and neat work, subscribed.
     
    Dennis Lacy likes this.
  19. rod1
    Joined: Jan 18, 2009
    Posts: 1,377

    rod1
    ALLIANCE MEMBER

    What a Great build. Thanks for taking the time to show the details.
     
    Dennis Lacy likes this.
  20. banjorear
    Joined: Jul 30, 2004
    Posts: 4,601

    banjorear
    Member

    Looks great. Thanks for sharing.
     
    continentaljohn and Dennis Lacy like this.
  21. Andy
    Joined: Nov 17, 2002
    Posts: 5,227

    Andy
    Member

    You might as well have left the center out. The torsional stiffness is basically determined by the cross
    section area and the material properties. You have removed most of the area.
    Nice work though.
     
    Dennis Lacy and X38 like this.
  22. Dennis Lacy
    Joined: Apr 27, 2008
    Posts: 1,407

    Dennis Lacy
    Member

    Ah, right you are. BUT, I’m not done yet… ;)
     
    BigJoeArt, rod1, RICH B and 2 others like this.
  23. scotti32
    Joined: Jul 13, 2009
    Posts: 284

    scotti32
    Member

    Very cool build.
     
    Dennis Lacy likes this.
  24. glennpm
    Joined: Mar 29, 2015
    Posts: 188

    glennpm

    Beautiful, professional work!
     
    continentaljohn and Dennis Lacy like this.
  25. 1940Willys
    Joined: Feb 3, 2011
    Posts: 841

    1940Willys
    Member

    I Like it!
     
    Dennis Lacy likes this.
  26. 34 5W Paul
    Joined: Mar 27, 2020
    Posts: 353

    34 5W Paul
    Member
    from Fresno CA

    If the goal were to maintain 100% of Henry's torsional stiffness in the X brace center while reducing its cross section, what would you do? Go thicker with the new u-shaped insert? Replace the stock lower pan on the center with a thicker one? Add some ties between the new U shaped insert and the lower reinforcement pan? Asking for a friend...
     
    Dennis Lacy likes this.
  27. alchemy
    Joined: Sep 27, 2002
    Posts: 21,415

    alchemy
    Member

    I’d make a top plate.
     
  28. AmishMike
    Joined: Mar 27, 2014
    Posts: 1,138

    AmishMike
    Member

    Fit the trans then put 2 1/2 square tubes across top of saddle. Still can slid off rear of trans for maintenance
     
    Dennis Lacy likes this.
  29. Atwater Mike
    Joined: May 31, 2002
    Posts: 11,619

    Atwater Mike
    Member

    Great project, Dennis.
    Did you ever get to count the ratios in the 4 different gears? (some are swearing by a 'Granny low', but the former installation in the Facel Fords were passenger car.)
     
    Dennis Lacy and Outback like this.
  30. If that Facel Vega trans came out of a Chrysler powered car, it won't have a granny first.
     
    Dennis Lacy and Outback like this.

Share This Page

Register now to get rid of these ads!

Archive

Copyright © 1995-2021 The Jalopy Journal: Steal our stuff, we'll kick your teeth in. Terms of Service. Privacy Policy.

Atomic Industry
Forum software by XenForo™ ©2010-2014 XenForo Ltd.