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Technical Rebuilt 302 has no get up! Help.

Discussion in 'The Hokey Ass Message Board' started by Brandon141, Apr 15, 2024.

  1. Brandon141
    Joined: Aug 25, 2021
    Posts: 67

    Brandon141

    Got into the motor!
    #1
     

    Attached Files:

  2. RmK57
    Joined: Dec 31, 2008
    Posts: 2,957

    RmK57
    Member

    Does that intake valve look really bent? Or is the camera angle?
     
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  3. Sharpone
    Joined: Jul 25, 2022
    Posts: 1,782

    Sharpone
    Member

    It looks like it’s canted, like it’s not in the same plane as the other intake. Brandon141 can you get a top side picture of that head? The valves don’t look right
    Dan
     
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  4. Budget36
    Joined: Nov 29, 2014
    Posts: 14,753

    Budget36
    Member

    And post “full image”. Can’t expand a thumb nail on my phone, it washes out and goes away.
     
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  5. Kerrynzl
    Joined: Jun 20, 2010
    Posts: 3,433

    Kerrynzl
    Member

    tip some gasoline into number one chamber and see if it leaks past the valves
     
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  6. Brandon141
    Joined: Aug 25, 2021
    Posts: 67

    Brandon141

    So the piston looks fine. I poured some fuel into the chamber on the head and waited like ten minutes. No leak down. I’m going to pull the motor and go through, change rings on 1 and 6. And change the cam. Sucks, but my mistakes caused this. Live and learn!!! I’m thinking B or E cam with 4:11 gears.
     
  7. lostn51
    Joined: Jan 24, 2008
    Posts: 2,462

    lostn51
    ALLIANCE MEMBER
    from Tennessee

    Who put the rings on the pistons? If you look closely at #1 you can see a gap between 6 and 7 o’clock and there are scores in the cylinder around the 4 o’clock position. Sure is a lot of oil in that cylinder too. I’d have to be there in person but I’m pretty sure that you might have the rings in the wrong spots on a couple of pistons
     
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  8. Brandon141
    Joined: Aug 25, 2021
    Posts: 67

    Brandon141

    I was told the block only had 4000 miles. I should’ve checked the compression when I had the motor on the stand.
     
  9. Brandon141
    Joined: Aug 25, 2021
    Posts: 67

    Brandon141

  10. Sharpone
    Joined: Jul 25, 2022
    Posts: 1,782

    Sharpone
    Member

    Brandon you might get a fellow HAMBer to help in person , just post your general location , area of state or town and state, if they are close they can PM you and you can trade phone #s or whatever.A lot of us are retired and always looking for a good outing.
    Dan
     
  11. lostn51
    Joined: Jan 24, 2008
    Posts: 2,462

    lostn51
    ALLIANCE MEMBER
    from Tennessee

    That’s what I’m saying!!!!;););)
     
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  12. Brandon141
    Joined: Aug 25, 2021
    Posts: 67

    Brandon141

    I am located in the “thumb” of Michigan.
     
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  13. lostn51
    Joined: Jan 24, 2008
    Posts: 2,462

    lostn51
    ALLIANCE MEMBER
    from Tennessee

    Crap I’m in the arm pit of Tennessee lol:oops:

    I know there has to be some folks around you that would love to come over and help you out. I know if I was closer I’d love to turn some wrenches :)
     
  14. seb fontana
    Joined: Sep 1, 2005
    Posts: 8,955

    seb fontana
    Member
    from ct

    Aren't those pistons for a "twisted Wedge" head?
     
  15. I have an e303 in my 87 5.0 block, AOD, and 3:50 gears. My 55 is a mild custom and not a street brawler but it cruises down the highway nicely. 4:11 may be the ticket for what you are after. Good luck, I'll be following along.
     
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  16. Kerrynzl
    Joined: Jun 20, 2010
    Posts: 3,433

    Kerrynzl
    Member

    While the head is off,. now would be a good time to check TDC against the marks on the balancer!
     
  17. GlassThamesDoug
    Joined: May 25, 2008
    Posts: 1,783

    GlassThamesDoug
    Member

    4k miles with a Blower? Like the one I pulled out of a FOX body...was shot, broken rings, junk heads.

    Bought a 380hp 306 roller from blueprint with Dyno Sheet. Strong unner around town. Heads looked like yours.

    I got damaged blower for labor, but had to sink $700 in it.
     
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  18. GlassThamesDoug
    Joined: May 25, 2008
    Posts: 1,783

    GlassThamesDoug
    Member

    Could have brought it to Detroit Auto Rama could of checked it out in Parking lot. Lot of rodders there.
     
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  19. GlassThamesDoug
    Joined: May 25, 2008
    Posts: 1,783

    GlassThamesDoug
    Member

    O-psi is always valve bent, or hole in piston
    Broken rings make pressure.

    Your finding problem, good.
     
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  20. Budget36
    Joined: Nov 29, 2014
    Posts: 14,753

    Budget36
    Member

    Brandon verified the valves are sealing with gas.
    I don’t think zero compression could be had with a bad ring/worn hole, could it, if the valves are sealing? I think (again think) it’s possible the cam timing isn’t correct, and even really think the valves were not adjusted properly.
    But I do have a friend who pulled his heads for a valve job for a miss he couldn’t find.
    He still had the miss after the heads were back on.
    Plug wires on the wrong plugs.
     
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  21. GlassThamesDoug
    Joined: May 25, 2008
    Posts: 1,783

    GlassThamesDoug
    Member

    Zero is a massive leak, piston if valves are OK.

    Multiple top, intermediate rings produce some psi. ZERO is hard to create. HARDWARE. Pull piston, cast, might be porus... forgot to ask, piston is reaching TDC... bent rod Q.
     
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  22. Budget36
    Joined: Nov 29, 2014
    Posts: 14,753

    Budget36
    Member

    I get ya, but kind of a stretch there.
    Odd thing is “fired up and idled fine” if I recall correctly.
     
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  23. GlassThamesDoug
    Joined: May 25, 2008
    Posts: 1,783

    GlassThamesDoug
    Member

    I bought a 283 (sold as fresh, running) for a mild blower build, 2cyl had zero, 2 around 50, pulled it down, rusted cyl, had stuck rings, gasket material under valve faces, a real screw job. Rebuilt it, honed, Runs great now carbureted.
     
    Last edited: Apr 24, 2024
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  24. Moriarity
    Joined: Apr 11, 2001
    Posts: 34,585

    Moriarity
    SUPER MODERATOR
    Staff Member

    too bad it got pulled apart too soon, could have been a mis adjusted rocker arm holding a valve open, now we will not know.....the above comments are correct 0 psi should be an obvious (big) problem
     
  25. Brandon141
    Joined: Aug 25, 2021
    Posts: 67

    Brandon141

    I poured fuel onto the valves, no leaks detected and I let it sit there awhile. And I admit, I got too eager and pulled the head before totally loosening up the rockers and did a comp test. I might throw the head back on and see if I get any pressure from #1 with no pushrods on the rockers.
     
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  26. 1971BB427
    Joined: Mar 6, 2010
    Posts: 9,359

    1971BB427
    Member
    from Oregon

    Shame you pulled it down, but not as bad as if you had pulled the engine out and began total rebuild.
    I'd put the heads back on with the same gaskets (if they look undamaged?) and torque them down. Then adjust all the valves at zero lash before doing another compression test. If compression comes back good on all cylinders then buy new head gaskets and install them, and do a proper valve adjustment.
     
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  27. GlassThamesDoug
    Joined: May 25, 2008
    Posts: 1,783

    GlassThamesDoug
    Member

    Not a bad idea...
     
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  28. Kerrynzl
    Joined: Jun 20, 2010
    Posts: 3,433

    Kerrynzl
    Member

    They are stock 5.0 pistons.
    From 86-91 Ford used TRW forged, from mid 91 Ford used Hypereutectic
    The junkyard method to tell is look at the colour of the oilpan [Black=Forged, Grey= Hypers]

    Twisted Wedge heads use stock pistons, they were clever by moving the valve location/angle so the pistons didn't get romantically involved with the valves

    Just run some Loctite around the fire ring of the old head gasket and re-install [wait an hour or so]
    Then compression test number one again.
    This saves buying a new head gasket just to do the compression test.

    If all is OK , then replace the gasket on the final install
    I would adjust the lifters with no preload [or 0.010" lash] for the compression test
     
  29. 50 Merc Man
    Joined: Aug 2, 2020
    Posts: 512

    50 Merc Man
    Member

    Carb too small more than likely
     
  30. Moriarity
    Joined: Apr 11, 2001
    Posts: 34,585

    Moriarity
    SUPER MODERATOR
    Staff Member

    better go back and read the entire thread, he found 0 compression on one cylinder
     

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