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Projects 1948 Plymouth Coupe Custom build

Discussion in 'Traditional Customs' started by Hillbilly Werewolf, Dec 29, 2021.

  1. gene-koning
    Joined: Oct 28, 2016
    Posts: 4,577

    gene-koning
    Member

    Car looks great!
     
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  2. Vinnie Barbarino
    Joined: Dec 9, 2023
    Posts: 7

    Vinnie Barbarino
    Member

    These are all great looking cars! I just sold mine to start my model A sedan project. I built the flathead 6 race cam and all.
    Good to see some Mopars again.
     

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  3. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    Been a while since a real update, spent most of last year working an average of 60 hours a week, so getting work done on the car has been slow going. I did manage to drive the Plymouth 1-2 days a week most of the year. That really got me thinking about all the work I need to get done on it!
    First priority is getting this BW OD rebuilt and installed. Mid December I started my "One piece at a time" plan, and rebuilt the selector mechanism. 20231220_122727.jpg 20240112_125230.jpg
    With some machine work and welding, I managed to take .015" of slop out of a couple places, and polished all of the rubbing surfaces. I also found earlier selector levers that are much shorter, hopefully they will work to reduce lever travel.
    I have now started on the rest of the trans. It is a little slow, between only working on it during my lunch breaks, and tracking down the parts to switch to the stronger "strut" synchros. 20240126_135809.jpg 20240130_123520.jpg 20240113_092436.jpg 20240126_135813.jpg 20240203_091250.jpg

    Last week I got sick of the gas smell that has plagued the car for a couple months, so I swapped the leaky Carter Ball and Ball for the Carter WA-1 I rebuilt over a year ago. Went surprisingly well, and with a little tuning runs quite well. Seems much smoother than the previous carb, with less of a "wet sucking sound". While tuning, I noticed that it was producing fuel mist like a smoke machine, vs the slightly broken up drip of the B&B.
    Only down side is that it doesnt seem to like cold starts, so yesterday I finally installed a choke cable. The B&B went 2 years of chokeless cold starts.
    I think it could use a little more tuning, Idle is a little too rich, but leaned out it acts like it needs more accelerator pump.
    20240209_150919.jpg 20240209_150926.jpg
    I took a couple vacation days for my anniversary and birthday, so I finally took it to a tire shop and had the wheels balanced. All were a little bent, so we put the best on the front. 3 out of 4 were out of balance. Now no more vibration above 60. 20240215_135742.jpg

    This allowed me to hit a new top speed on the expressway: 86 mph. Power was -just- starting to break up, maybe a little valve float? Keep in mind this is with 3.9 rear gears and the standard 3 speed still. I do not understand why so many people think these cars can't run 65...I run 70 with traffic routinely, with power to spare.

    Next up I am going to make a second try to get my dual point distributor installed, hopefully I can get a condenser to survive this time....​
     
    Last edited: Feb 16, 2024
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  4. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    Well, it is nearly time for me to wrap this thing up.
    My wife and I have decided to make some big life changes: I have quit my job and we are selling everything and moving our two young boys and us to southeast Asia, for the foreseeable future.
    Unfortunately the Plymouth cannot come along, so I am going to tidy up all the loose ends I can, and get it sold.
    Luckily, the area we are going has a big vintage car scene, and mechanics, paint and upholstery are affordable.
    Unfortunately, it is a slim chance that the Plymouth replacement will be HAMB friendly.

    SO! All that out of the way: What have I gotten done the last six months?
    A few things.
    I got the dual point distributor and Mallory "best" coil installed and working.
    20241017_180247.jpg
    After some trouble with the battery, and a reckless 12v to 6v jumpstart or two, I installed a new, larger 6V battery, a NOS autolite solinoid, and a set of custom 00 gauge battery and starter cables. A new battery hold down, some stickers and some red paint has it looking right at home. It spins over faster than ever, so I am very pleased. 20241017_141457.jpg


    I swapped back on a fresh B&B carter, because I could not tune out the off idle stumble.
    It had been built by a self proclaimed expert, but is a total mess.
    So after a few months of poor running, leaking and being a jet too rich, I finally found the time to sit down the the 413s WA-1 again. Poking around I found that I had mistakenly put the accelerator check ball in the wrong spot (under the vacuum piston is NOT where it goes)
    Unsurprisingly, the off idle stumble is gone, and am happy to be rid of the Ball & Ball once again. 20241017_180234.jpg 20241017_141457.jpg

    I have been chasing a misfire since installing the B&B, I assumed that it was loading up the plugs, but after going back to the WA-1, the miss is still there, although better. I pulled and examined all the spark plugs, and found that 5 looked good (although a little rich) but one had a small crack in the insulator, right by the electrode. I believe this is grounding out under high load, causing the miss. This evening I will find a spare set of plugs for it to install.
     
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  5. RodStRace
    Joined: Dec 7, 2007
    Posts: 5,554

    RodStRace
    Member

    Best of luck to you and your family on the major life change. Sorry the Plymouth has to go, but family first. If it ends up you can dip back into autos as a hobby later, perhaps you can post over it the OT section.
     
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  6. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    I hadn't seen the OT section, I will be sure to post some stuff there.
    It seems that the housing market is dead for the year, we are going to survive here till spring and try again. Son in the meantime, it is back to working on the Plymouth. Besides, its my only car now!
    Plugs fixed my misfire, and it has been running sweet ever since.
    So naturally, I had to go and make it inoperable right away! Yesterday I started on installing the BW Overdrive I rebuilt last spring, and a fresh clutch.
    20241109_164233.jpg
    I got the old transmission out with little fuss, other than I had to sacrifice a section of my exhaust that ran across the tail of the trans.
    20241109_153303.jpg 20241109_173059.jpg
    I will also be installing a fresh clutch linkage and less worn out shifter linkage. 20241109_164249.jpg
    20241109_174643.jpg 20241109_174719.jpg 20241109_174651.jpg

    Found why the transmission leaked from the front: whoever installed the trans last did not put the gasket between it and the bellhousing.
    Today I am going to get the clutch out and maybe the flywheel. I am also going to replace the rear motor mounts and start cleaning and repairing all the wornout linkage bits.
     

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  7. George
    Joined: Jan 1, 2005
    Posts: 7,818

    George
    Member

    Weld some header flanges on so you can drop that piece of ex pipe when needed.
     
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  8. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    Thats a great idea, but I think I am going to have to reroute that section anyway, it is almost up tight to the tailshaft of the stock 3spd, but the r10 OD has a fat ass.
    I will see if I can manage flanges on the new section though
     
  9. Budget36
    Joined: Nov 29, 2014
    Posts: 14,441

    Budget36
    Member

    Best of luck on the move.
    Bummer you can’t take the Plymouth with you.
     
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  10. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    I recently found a vlog of a british couple who drove across SE asia in their UK licenced van. I need to figure out if I could do something similar, I would LOVE to have the Plymouth as our Thailand roadrip car.
    Anyway, I got the clutch and flywheel out today. They had 3 matching hot spots and oil on the hub of the disc, so that explains the chatter.
    Do yall think this flywheel can be saved? The hot spots have some fissures, but it feels pretty flat still. 20241110_135738.jpg 20241110_183941.jpg 20241110_183946.jpg 20241110_183951.jpg 20241110_184004.jpg

    The second flywheel is off a 230, so the flange depth is around .065" too deep.
    Should I go pull the flywheel that is on my spare engine and bring both to the machine shop?
     
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  11. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    Luckily, my spare came off easy, and was not cooked. Dropped it and my pressure plate off monday at the machine shop, they ground it and balance matched the PP to the wheel.
    I found a 10" diaphragm clutch that is supposed to fit to upgrade from the stock 9" borg&beck. The FW is drilled for both sizes from the factory, but the bigger pattern uses 3/8 bolts instead of the 5/16" that the stock clutch uses. A set of ARP SBC bolts fit perfectly.
    However, when I went to install it in the car, I found that the PP hits the bell, when the clutch disk is in place. Without it, it fits fine.
    I am hoping to grind the 2 spots (clutch fork windows) enough to let me install it. Definitely frustrating, as no one mentioned this issue when I researched this clutch set up. 20241115_165730.jpg
     
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  12. RodStRace
    Joined: Dec 7, 2007
    Posts: 5,554

    RodStRace
    Member

    looks like 130-2201 is the ARP number, for the old eyes out there.
    Sorry to hear it's going to take work to get things to fit.
    Documenting this at least might help the next rodder to go down the path.

    BTW, I've gone back and read the build. You've done the car proud! It's really nice and with all the small and large fixes you have done it is not just a looker but a driver!
     
    Last edited: Nov 16, 2024
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  13. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    I appreciate that. Sometimes it is easy to forget how much work we all put into these old things.
    Yup, that is the correct number. Those are the 3/8" bolts for the big clutch, the small pattern uses 5/16 bolts. ARP should have something that would work for those too. 1" under head length is pretty much perfect.

    I am going to tackle that bellhousing tomorrow, it is going to work, somehow!
     
    Last edited: Nov 16, 2024
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  14. Hillbilly Werewolf
    Joined: Dec 13, 2007
    Posts: 535

    Hillbilly Werewolf
    Member

    The truck bells must have a touch more space in em or have the clutch fork windows laid out differently.

    I was able to use my die grinder and a burr to cut the clearance I needed to install everything.

    I forgot to take a victory picture with the transmission in.

    I will get all the driveshaft, linkages and OD wiring harness installed tomorrow.
    20241117_125131.jpg 20241117_124049.jpg 20241117_125153.jpg
    20241119_181332.jpg
     
    Last edited: Nov 21, 2024 at 5:49 AM
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