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Projects A/V8 speedster ‘Sat Nite Spcl’

Discussion in 'Traditional Hot Rods' started by Oldtmtech, Jul 28, 2022.

  1. For the American hot rodder it might not be of much interest but I have always been drawn to these cars
    The great thing about these older books is that the authors usually had firsthand knowledge of the cars that they were writing about
    Very few pictures just a lot of in-depth technical information IMG_4510.jpeg the authors have great credentials IMG_4511.jpeg I found this copy pretty cheap with a company called thriftbooks
    I also have several other old books that cover these cars written by people that actually owned and drove them
     
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  2. When this project was started it was just going to be a stationary engine (talk about losing focus) I had picked up a offenhauser 2x2 intake but it didn’t have the look I wanted
    I really like the’34 intake and have already done alot of porting for a single carb and not wanting to mess with that manifold went ahead and picked up another’34 manifold
    I believe you started to see the y type carb adapter coming out in the late’30s so decided to check out vintage speeds adapter IMG_4535.jpeg IMG_4538.jpeg IMG_4541.jpeg for the price I am really happy
    It has a 5 1/2” carb spacing IMG_4545.jpeg IMG_4546.jpeg IMG_4548.jpeg Will need to do some matching for the carbs IMG_4540.jpeg and then open up the manifold face IMG_4542.jpeg and then on the manifold I will do the runner porting like I did with the original but then open up the carb mount to an open plenum IMG_4544.jpeg I am curious what the Edelbrock sling shot manifold looks like on the inside but have failed in finding any pictures IMG_4551.jpeg am assuming they kept a dual plane setup but if anyone has pictures please post them
    If I only knew how to photoshop IMG_1397.jpeg 583B3CE5-5731-436B-A97D-DC56740DF8B9.jpeg
     
  3. torpedo jones
    Joined: Feb 7, 2005
    Posts: 12

    torpedo jones
    Member

    Cool build, can’t wait to see more! What’s the book with the model t ascot racer you have shown in the beginning?
     
  4. Thanks
    Here you go a coffee table book lots of good pictures IMG_4602.jpeg IMG_4603.jpeg IMG_4604.jpeg A good day on YouTube today
    Had the Prescott hill climb and bonneville
     
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  5. Because of tropical storm Debby I had a couple of days in the basement on the milling machine to work on the vintage speed intake
    First had to do a little dremel work for clearance IMG_4612.jpeg used a 1.250” end mill to open up the ports IMG_4613.jpeg IMG_4614.jpeg IMG_4615.jpeg IMG_4617.jpeg IMG_4619.jpeg will do some die grinding to blend in
    The intake side was a little offset on the casting IMG_4625.jpeg flycut the mating surfaces IMG_4628.jpeg IMG_4629.jpeg now for the intake manifold
    I had got this manifold because I didn’t want to mess up my other intake wanted to see how these were cast
    So here is how the exhaust heat riser is cast IMG_4620.jpeg IMG_4621.jpeg I’ve blocked off the exhaust crossover in the block so I can save this with a little jb weld
    I now know that I can take my good manifold and just taper the ports on the upper 1/2”
    This manifold also had some corrosion on the face IMG_4635.jpeg IMG_4636.jpeg so this was a good test of the fly cutter I had made several years ago just for when I need to mill my heads IMG_4637.jpeg IMG_4642.jpeg https://youtube.com/shorts/uj5G8NBi0Cs?si=3vk81_K6g5GBOF6e image.jpg will need to port the runners then this combination intake will be ready for testing when I have the engine running
    Will be taking a little break from this project got to start preparing for my local steam and gas show in a couple of weeks
    Till next time
     
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  6. An ongoing project has been the generator
    Like to thank Steve Blancard who I met at the swap meet back in the spring you can see his short but informative videos on generator repair here. https://youtube.com/@steveblancard5566?si=j_r1c97fKG2FIrgp
    Steve kindly talked me out of using the solid state cut out and just adjusting the original
    Here it is after adjusting
    https://youtube.com/shorts/Fh_mU8E1mxQ?feature=shared

    https://youtube.com/shorts/1-r7QgjKnB8?feature=shared
    Brought out my dads old growler to check the armature
    https://youtube.com/shorts/tkkhzsy5mVo?feature=shared
    so I got a shorted armature and that’s where my generator has stalled out for now but you never know when parts will appear
     
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  7. While the intake was mounted on the mill went ahead and blocked off the exhaust crossover IMG_4655.jpeg IMG_4656.jpeg IMG_4657.jpeg
     
  8. We truly blessed with great weather this past week so I took the opportunity and got the engine painted
    Not some of my best work but not my worst either
    The little air compressor I am currently using just can’t keep up with my old siphon gun
    I’m still adapting to my new work area IMG_4660.jpeg IMG_4665.jpeg IMG_4666.jpeg IMG_4674.jpeg IMG_4676.jpeg Engine will now be put back on the engine stand and be transferred to my clean engine assembly room (my man cave basement)
    So this winter I hope to get the assembly done
     
  9. Needed a way to store the trans
    Looked thru the scrap pile for inspiration and found a brake drum from my daily driver
    It’s the type with built in bearings
    Machined it flat then welded in a piece of pipe
    This works great it makes a base that is small but really stable with the transmission on top and it still rotates IMG_4693.jpeg IMG_4694.jpeg IMG_4702.jpeg My’35 swan shifter IMG_4707.jpeg IMG_4705.jpeg
     
  10. Previously I had machined about 4.5 lbs off of the flywheel so I used Mart’s method of balancing https://youtube.com/@martsgarage?si=vS9HObNVopLemhMC
    I was afraid of screwing up so the hole I drilled I used a letter F drill which is the hole size for a 5/16” tap
    I could always tap the hole and thread metal back in
    The first hole is 1” deep the second is just a starter drill IMG_4699.jpeg IMG_4700.jpeg I feel real confident because my holes ended up in between what was left from the original balancing holes IMG_4709.jpeg IMG_4710.jpeg my holes were even biased towards the bigger of the 2
    I am going to try and experiment further
    I found a bearing that fits on the front of the crank IMG_4708.jpeg I’m then going to mount the crank with flywheel attached in the lathe so it will be supported on each end with a ball bearing and see if everything is still balanced
    Stay tuned
     
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  11. Continuing with the generator I went to install the field coils and found that the new screws that I had bought that were supposed to be for all flathead v8s were not the correct size
    Apparently later v8 had 7/16 threads my generator had 3/8 threads the same as model A I think and not wanting to buy just 2 bolts went to use some screws from inventory and found that the generator didn’t use a standard counter sink taper
    Standard taper being 82* generator at 60* IMG_4767.jpeg decided to machine a new taper but was confused about how to set the compound on the lathe so had to draw it out IMG_4778.jpeg IMG_4779.jpeg used a collet to hold the screw IMG_4766.jpeg IMG_4768.jpeg new taper IMG_4770.jpeg installed IMG_4772.jpeg interesting new part being delivered tomorrow stay tuned
     
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  12. I got 2 parts deliveries this week
    The first being another vintage speed manifold
    This must be a early casting because it’s actually a true dual plane casting
    After some cleanup I will be able to bolt this up to my original manifold with no modifications
    This is what I was looking for in the beginning IMG_4858.jpeg IMG_4860.jpeg IMG_4861.jpeg IMG_4862.jpeg IMG_4863.jpeg The 2nd part is a’38-‘39 generator armature
    Been wanting to finish the generator but haven’t found any affordable armatures
    After doing some research found this one pretty cheap and decided to see if I can machine it to fit IMG_4852.jpeg IMG_4854.jpeg IMG_4855.jpeg check out how many times the old one has been turned IMG_4851.jpeg the thread is the same just the main diameter and the seal diameter are different with just a little bit more length needed for the bearings I think I can just trim.040” off the key instead of cutting the key seat deeper (I would have to buy a key seat cutter)
    Got it set up in the lathe just doing more thinking before I start making cuts
    Also I disassembled the starter everything looked great so I cleaned greased and reassembled
    I then noticed that the terminal bolt was stripped I rethreaded it but I think what I will do is cut it off and install a coupling nut in place of the first nut and then either use a bolt or stud to attach the cable The thread under the first nut is ok IMG_4867.jpeg You can then hold the coupling nut with a wrench when you tighten the cable to prevent everything from turning IMG_4865.jpeg
     

    Attached Files:

  13. Posting in real time today
    Started turning the armature down and discovered a few things
    The split sleeve came loose so I loctited it in place only to discover that the dimension of the shaft was already correct for the felt seal IMG_4868.jpeg IMG_4870.jpeg IMG_4869.jpeg I’m getting better with my machining skills and got the proper finish dimension and because I had indicated the tail stock I had no taper (probably a first for me) IMG_4856.jpeg IMG_4871.jpeg IMG_4872.jpeg IMG_4874.jpeg fortunately I started looking at the key before starting to machine it
    It works perfectly without modification
    It’s like this armature started life as a earlier version IMG_4877.jpeg IMG_4878.jpeg
     
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  14. Some finishing touches IMG_4883.jpeg IMG_4885.jpeg
     
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  15. I don’t have much to report but I have gotten in some new hardware for the main caps and rods
    On these early engines the main cap bolts go thru the block from the cam valley IMG_4974.jpeg I matched up some new bolts to replace the square head ones IMG_4964.jpeg IMG_4968.jpeg they came in stamped arp so that’s good
    Some new nuts too IMG_4965.jpeg IMG_4972.jpeg the threads feel really smooth should get good torque values
    New con rod nuts since a socket doesn’t fit well on the originals IMG_4967.jpeg IMG_4970.jpeg IMG_4979.jpeg IMG_4981.jpeg
     
  16. Got the crankshaft cleaned using some oven cleaner
    I’ve read to take out the oil gallery plugs but these early cranks don’t have any plugs IMG_5079.jpeg I’ve actually had a hard time finding info on these early engines
    The 21 stud motors particularly pre insert main bearing just don’t have the following
    What was the first thing you did to a’34 ford you replaced that motor with a late model flathead this is hotrodding after all
    I had previously polished the crank when I had disassembled the engine that was when I measured the clearances
    This project would have never happened if it needed new Babbitt
    Crank clearance measured.002-.0025 “ with the shims still installed
    This motor has had the crank turned and new Babbitt poured in its past IMG_5082.jpeg IMG_5080.jpeg mounted the crank and flywheel in the lathe on ball bearings
    IMG_5073.jpeg Gave me an appreciation for crank balancing and bob weights
    It would always settle with the rod journals equalized IMG_5075.jpeg IMG_5076.jpeg IMG_5077.jpeg I think I will deburr the crank just to protect my hands while I’m working on the bottom end IMG_5078.jpeg
     
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  17. WARNING
    This maybe a very long post so read at your own risk of being totally confused as I’m sure I will be just writing it
    While researching generators (* seeprevious posts) I found that there are 3 basic types
    ‘33-‘39 (‘38-‘39 being odd*) 1/2”thread on end of armature, small diameter case
    ‘40-‘48 bigger case and armature with big diameter thread (possibly 17 mm haven’t actually measured ,electric motors bearings are always metric just like spark plugs so you never know) IMG_5133.jpeg IMG_5134.jpeg ‘49-‘53 the ones with the strap mount IMG_5135.jpeg I’ve been thinking about using a mid mounted fan for radiator clearance but using a early generator IMG_0403.jpeg CB4205AD-39B8-4D89-9854-AE828A0F5FB5.jpeg probably will have distributor clearance problems but I won’t know that until I get the motor assembled
    Thought about using the strap mount and welding to the front end plate but that looked like it would be a mess
    Thought about welding pads to the front end plate IMG_5120.jpeg that’s probably not a bad idea
    Picked up a’42-‘48 end plate #21A-10139 and started machining (remember from above the bigger case diameter) IMG_5093.jpeg IMG_5094.jpeg IMG_5098.jpeg IMG_5100.jpeg IMG_5096.jpeg Then had to put in new threaded holes for assembly (find myself using the rotary table a lot) IMG_5106.jpeg IMG_5107.jpeg standard replacement bearing is a 6203-2rs
    (17mm bore x 40mm od x 12mm)
    I’m using the small diameter shaft so the bearing you need is 6203-15-2rs
    (15mm bore x 40mm x 12 mm wide)
    IMG_5121.jpeg Had to turn the armature.250” further (using my burnt up armature for fitting purposes) IMG_5129.jpeg assembled together IMG_5111.jpeg then had to make a spacer.750” long to get the pulley proper distance IMG_5114.jpeg IMG_5115.jpeg IMG_5131.jpeg IMG_5132.jpeg used the old bolt holes to index the end plate IMG_5126.jpeg IMG_5127.jpeg IMG_5128.jpeg I would be driving the fan off of the generator (no room for an extra sheave on the crank pulley)
    So would be machining a pulley for the generator
    Will the generator shaft and bearing take the stress? Don’t know but using pulley diameters I can really slow the fan down
    I don’t think the multi grove generator pulleys would have the proper spacing
    But I’m getting ahead of myself need to get the motor assembled and running IMG_5116.jpeg IMG_5117.jpeg IMG_5122.jpeg IMG_5124.jpeg
     
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  18. Fabber McGee
    Joined: Nov 22, 2013
    Posts: 1,386

    Fabber McGee
    Member

    Lots of good work there. Seems like it might be difficult to get a replacement in Valentine, Nebraska on a Sunday afternoon.
     
    Outback likes this.
  19. Happy thanksgiving everyone
    Bringing you an update while you wait for your turkey dinner
    Got the crankshaft deburred ,the oil passages cleaned out and the flywheel threads chased
    It’s just waiting for a final cleaning before installing
    Turned my attention to the main caps
    After 90 years the nut surfaces are quite distorted and it looks like somebody has taken a chisel to a couple of them IMG_5159.jpeg took a skim cut to clean up the surfaces also reamed out the holes where they were distorted IMG_5160.jpeg IMG_5161.jpeg IMG_5163.jpeg Next I thought that since I had a couple of spare parts from my generator project (front plate,old armature) that I might try to make a idler pulley or what I believe was called a cutdown generator
    Found this old piece in dads scrap (he would disassemble old parts and keep anything that he might want to use) IMG_5169.jpeg the little end is the correct size so cut it off
    IMG_5171.jpeg IMG_5172.jpeg IMG_5173.jpeg Will still need to weld up the split IMG_5176.jpeg looks good bolted together IMG_5178.jpeg IMG_5179.jpeg turned my attention to the armature
    Removed the copper then beat the remaining off the shaft IMG_5164.jpeg IMG_5165.jpeg IMG_5180.jpeg will have to cut the shaft off
    Then turn the end down to.625”for the end bushing
    I’m hoping the shaft will clean up at.625” that would make life easier IMG_5181.jpeg I can make a new bushing but prefer to use a unmodified end plate (complete with brush holders)
    Can also sleeve the shaft
    I think this would be useful especially on the run stand where I could use a 12 volt battery and not having to buy a 6 volt battery just for running the engine
    Have a great day everyone IMG_5182.jpeg
     
  20. Deutscher
    Joined: Nov 12, 2024
    Posts: 91

    Deutscher
    Member
    from Germany

    Wow, absolute genius
    Greetings Harald
     
    dmar836 likes this.
  21. Thanks everyone
    Just happy to show my journey and by posting once a week it makes me come up with content so it keeps the project moving forward
    Continuing the crank shaft installation
    Looking at the new bolts noticed that there was only 2 threads left before the nuts bottomed out
    Found some thick hardened washers and cut the od down to fit IMG_5186.jpeg IMG_5187.jpeg then to make it look original drilled safety wire holes IMG_5190.jpeg IMG_5192.jpeg IMG_5191.jpeg installed the oil galley plugs
    The front plug is a special plug that acts as a restricter going up to the oil pressure relief plunger IMG_5198.jpeg IMG_5201.jpeg the rear plug sits flush and gets covered by the oil pump gear housing so I cut down a socket head plug to replace the slotted plug IMG_5204.jpeg IMG_5203.jpeg then noticed that on the rear main what once was the drain tube IMG_5196.jpeg after much reading over on the ford barn
    Learned that the tube is often broken off and the little spot welds are factory to hold the tube in place because it’s a 1/2”-32 tpi straight thread IMG_5225.jpeg there’s much discussion about this tube and here is what I understand
    Ford did not have provision for crack case ventilation until’35 IMG_5223.jpeg so all the model A motors and the first years of the v8 had this tube that drains oil from the back of the rear bearing and extends all the way down into the oil pan so it is covered in oil
    The reason being is that without this tube crankcase pressure will go back up the drain hole and blow oil out the rear of the crankshaft (there being no rear main seals on these motors) with the tube extending down into the pan it allows the oil to drain back without it being subjected to the crankcase pressure IMG_5227.jpeg if you have a’35 or later block this tube is not as important because crankcase pressure has a easier way to exit the motor
    This motor only has 6 holes in the lifter valley for ventilation
    The front and rear of the crankshaft are not vented IMG_5228.jpeg Used a 1/4” npt tap to rethread the main cap and used a a compression fitting for 1/2” copper pipe
    I did open up the id of the fitting to make sure had good flow IMG_5216.jpeg IMG_5217.jpeg IMG_5219.jpeg IMG_5220.jpeg the tube is 1/2” from the bottom of the pan IMG_5221.jpeg so now you can remove the tube when working on the bottom end so the tube doesn’t get damaged
    I think that finishes up all the prep work for the crankshaft next I will actually be installing the crankshaft
    What a Christmas gift that will be IMG_5229.jpeg
     
  22. douglasb
    Joined: Feb 4, 2007
    Posts: 179

    douglasb
    Member

    The gen/idler looks good just add some way to retain the shaft inside, like a c clip or something I built one earlier this year and assumed it wouldn't stay together for some reason and at a light when taking off the fan pulled the shaft out and destroyed the fan/radiator 20240106_160749.jpg 20240106_190050.jpg 20240220_202959.jpg
     
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  23. tjm73
    Joined: Feb 17, 2006
    Posts: 3,599

    tjm73
    Member

    That steering wheel adapter is slick. But I think those allen bolts look out of place. I think some button head slot screws would look much more correct. The level of detail you're sharing is insane. Craftsmen level work. Look forward to the result.
    [​IMG]
     
    Oldtmtech likes this.
  24. Took some time this week to get the generator projects off of my work table which is also my pool table (would like to actually use it for its intended purpose )
    Got the armature shaft cut down for the modified generator IMG_5234.jpeg then got the mock up armature shaft machined for the cutdown generator IMG_5232.jpeg it had one groove that didn’t clean up I think it will do IMG_5230.jpeg IMG_5231.jpeg IMG_5233.jpeg these projects aren’t actually finished but they will be going back on a shelf for the time being IMG_5237.jpeg
     
  25. IMG_5246.jpeg The crankshaft is finally bolted in
    It feels really good
    Had to go buy me a new torque wrench also bought some assembly lubricant
    Checked the end play one final time IMG_5243.jpeg IMG_5241.jpeg safety wire IMG_5248.jpeg IMG_5247.jpeg starting to work on the connecting rods
    But now it’s time to play with some of my toys for the holidays IMG_5258.jpeg MERRY CHRISTMAS and a HAPPY NEW YEAR everyone be safe and I will talk to you in the new year
     
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  26. Happy New Year
    Thought I might reflect on what I have done this past year and where I’m heading in the new year
    Like to start with what I consider my mission statement
    The Preservation of Antique engines and equipment
    Key word being preservation
    The work I am putting into this’34 flathead is not about a restoration nor is it a proper rebuild it is simply about the preservation of a 90 year old engine that will be able to preform its original purpose without harming itself in the process
    I would love to properly do a rebuild but don’t have the time or money to do so, that being said if the time and money became available in the future (my time and money or someone else’s) the condition of this engine will be documented right here for anyone’s reference
    This project originally was about the motor and making a stationary engine for display purposes, the speedster part evolved out of that
    Still planning on the speedster part but will finish the stationary engine part first (the reason for the overbuilt run in stand)
    Let’s look at some of the engine sub assemblies
    Valve train
    Cam bearings. From a previous post you can see what this engine has so for a proper rebuild new bearings would have to be machined
    Camshaft. Very early in the process I found a eskenderian max-1 cam cheap as an open box (things were alot cheaper back then)
    I consider the max-1 a stock cam with more lift to help with the breathing issues
    “Zephyr” valve springs for the added lift
    Reconditioned by hand Johnson lifters (see a previous post) were already installed in engine
    Valves and guides. Reusing original valves with modifications and split guides
    ‘34 intake manifold (ported because I can)
    Block ‘34 pored Babbitt mains (.020” undersized) clearance checked (.002-.0025”)
    Ported (again because I can)
    Original painted on block IMG_3988.jpeg IMG_3990.jpeg cylinders were.030” over
    After honing IMG_5301.jpeg IMG_5302.jpeg
    will be using new.030”over domed pistons IMG_5323.jpeg with matching set of domed cylinder heads to replace the original flat top
    This engine had one aluminum head and one cast iron head
    The aluminum head had to be chiseled off and cracked in two (may have noticed in some of my photos) 583B3CE5-5731-436B-A97D-DC56740DF8B9.jpeg I thought that I had messed up the block but didn’t realize until today preparing for this post that the block damage already existed and was on the side with the cast iron head IMG_5318.jpeg IMG_5319.jpeg IMG_5320.jpeg as you can see in the head gasket
    For a rebuild it would need to be bored out and decked
    I do have a new set of head studs and these blocks have blind holes so no seepage problems with the head studs
    And I don’t see any damage that goes into the combustion chambers so head gaskets should seal
    Will be going into the connecting rods and full floating bearings for next weeks post
    For the upcoming year I hope to complete engine assembly and have it running on stand where I hope any problems will present themselves
    After the engine has been fully sorted out then I will look to working on the chassis again
    Here is a little montage of this past year https://youtube.com/shorts/ZbXHPfk9dH4?si=b-H4od4Zl8KPfKj1
    Things are moving quickly now so I am hoping for a productive new year
    I try to show everything I do including the mistakes so that it might help someone else
    You will want to see next week’s posting to learn with me about full floating flanged connecting rod bearings and the cheapest precision tool you will ever own IMG_5324.jpeg
     
    Last edited: Jan 1, 2025
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  27. Grumpy ole A
    Joined: Jun 22, 2023
    Posts: 193

    Grumpy ole A
    Member

    That is one of those hi-tech tools
     
  28. I’m back
    Mother Nature had other plans last week
    I will just do a short post on the rods this week
    Cleaned up the threads using a split die (you can adjust the amount of cut) mounted in a holder for the lathe IMG_5274.jpeg IMG_5275.jpeg checked the flatness of the end caps with a diamond file IMG_5277.jpeg IMG_5278.jpeg cleaned up the nut mating surface just like I did on the main caps IMG_5281.jpeg IMG_5283.jpeg useed a reamer to clean up the holes IMG_5284.jpeg had one rod that had obviously been reconditioned several times and the nut was bottoming out on the threads (the only rod that had strange wear pattern) IMG_5354.jpeg cut down some hardened washers for that rod IMG_5352.jpeg measured the big ends with dial bore gauge IMG_5349.jpeg the dial measures at.0001” so each number is only.001”
    It will scare you if you forget and the needle moves alot IMG_5350.jpeg The rods varied by up to.002” so in a perfect world these rods would need to be honed
    We will talk about rods and bearings next week
    This engine has a mismatch of rods
    I weighed them with the scales I had just bought from harbor freight
    Total weight ranged from 436 grams to 462 grams
    That’s 26 grams difference
    You can actually feel that in your hand
    I don’t know what the big and little end weights are but that is immaterial at this point
    Thought about using washers to add weight to the big end but 2 washers is only 3 grams (you start weighing everything when you have scales sometimes ignorance is bliss)
    I had numbered the rods when I disassembled the motor but somehow ended up with 2 number 6 rods (well 1 number 6 and 1 unreadable but definitely not the 7 it was supposed to be)
    I think it was mart’s garage that said you can tell how the rods go back by the witness marks and that helped
    The narrow grove goes towards the bearing flange IMG_5304.jpeg and the wide polished area goes where the rods mate together IMG_5305.jpeg plus I did take some notes when I disassembled that said the slit in the piston went with the slash marks on the rod image.jpg the small end bushings feel good with the new piston pins so at least they are okay
    I’m glad that I didn’t go wild with new parts and machine work in the beginning
    But I still feel that this motor will serve its purpose well and I’m getting a great education on ford flatheads
    Till next week stay safe out there
     
  29. Much has been written on floating bearings so I won’t get into what they are or how they function
    I’m just going to get into what I have learned
    Everyone agrees on how to adjust them a good wack with a soft mallet IMG_5391.jpeg IMG_5389.jpeg I found Ron’s book to have the best hands on explanations IMG_5382.jpeg although I found his way of measuring bearing thickness rather difficult IMG_5383.jpeg I think if I was serious about measuring a lot of bearings I would set up something like this with a dial indicator IMG_5384.jpeg IMG_5385.jpeg but in my case you will see it didn’t matter
    My crank journals are.010” under while my rods are standard
    I had purchased a couple bearings that I thought might work IMG_5387.jpeg these were advertised by the seller as having the bearing thickness that I needed and as hard as I tried I couldn’t get them to fit
    This set I bought because it had.010” under written on them IMG_5386.jpeg but again I couldn’t make them fit
    (All these were bought cheap I was trying to get some bearings in my hand to see what might work)
    After some research I found this posting on the ford barn IMG_5388.jpeg then I understood that you can’t buy I bearing by its thickness
    A bearing labeled JJ would have the same thickness as the bearing I really need which is a C
    Even a F or K would measure close
    The bearings I need are a C but the only set I have found is way out of my budget
    I could probably get a G set to work but they are probably more rare than the C
    (These are ford numbers you also have all the aftermarket numbers which I don’t know how to cross reference)
    So I am stuck with using the bearings that came out of the motor
    Of course I failed to mark the location of each bearing when I disassembled it so I went about fitting each bearing
    They all seemed tight on the crank journal so I spread them to get a good feel
    The connecting rods definitely have some excess clearance
    (This motor will be very friction free)
    I found this illustration in a repair manual that states that excessive clearance will cause excessive amount of oil to be thrown onto the cylinder walls
    If that is the only result of excessive clearance I can definitely live with that IMG_5392.jpeg I have taken measures to make sure that the oiling system is functioning properly
    (Cleaned all passages new pump and relief valve plunger and spring)
    The rods are now bolted in and the bearings are definitely free floating so I am pleased
     

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