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The Checker Adventure

Discussion in 'Off Topic Hot Rods & Customs' started by squirrel, Feb 4, 2025.

  1. mohr hp
    Joined: Nov 18, 2009
    Posts: 1,273

    mohr hp
    Member
    from Georgia

    This is all very entertaining. I had no idea of the event, looks like something I would do, except the cold part!
     
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  2. Crosley
    Joined: Mar 3, 2001
    Posts: 1,119

    Crosley
    Member
    from Aridzona

    Plans were for the inline 6 to come out for V8 conversion still?
     
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  3. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    yeah, that will start sometime soon...I have to do a few things first, like get a transmission together, etc.
     
  4. RodStRace
    Joined: Dec 7, 2007
    Posts: 6,539

    RodStRace
    Member

    Lying in bed last night, I thought
    'Wonder if the exhaust is coming apart inside and plugging'.
    Considering the work you put into the fuel system, and it's symptoms, it might be something to look at. They did do that even before cats.
     
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  5. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    The exhaust system is all new, except for the manifold.

    The weird thing is it still goes down the road at 75 mph, as long at it's not uphill or upwind.
     
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  6. RodStRace
    Joined: Dec 7, 2007
    Posts: 6,539

    RodStRace
    Member

    Well, shot that down! :)
    I'd plug in a vacuum gauge and monitor.
    Considering the size and weight, it SHOULD be able to pull at speed, but it might be at it's limits. The planned swap will fix it, but it's still an interesting puzzle.
    Air pump (engine) is not able to provide expected HP. Intake, exhaust, fuel, spark.
     
  7. Sharpone
    Joined: Jul 25, 2022
    Posts: 1,785

    Sharpone
    Member

    Dumb question. Will you be able to run Lemons with the new engines/transmission?
    Dan
     
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  8. TrailerTrashToo
    Joined: Jun 20, 2018
    Posts: 1,366

    TrailerTrashToo
    Member

    Any chance you have one of these little bastards in your carb?
    Sintered Bronze fuel filter.jpg
    Sintered bronze carburetor fuel filter - found behind the fuel input.

    Link: https://quadrajetparts.com/sintered-bronze-carburetor-fuel-filter-p-80.html

    My parent's 1972 Chevelle wagon had the same problem as a 4 year old car - Ran out of power under acceleration.

    Russ
     
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  9. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    yeah, they don't care, although you get more points if an old car has it's old engine.

    No filter in the carb, there's an inline filter before the pump.

    The symptoms don't include fuel starvation...that's pretty evident when it happens. Only once, since I installed the "new" fuel pickup in the tank, and it got pretty low on fuel, took 19 gallons to fill it. Fortunately it happened right before an exit with a gas station!
     
  10. RodStRace
    Joined: Dec 7, 2007
    Posts: 6,539

    RodStRace
    Member

    Those bronze filters did do a good job as a fine particle filter. Once you had big chunks, they were hopeless. Difference between gauze and screen door. ;)
    Not to mention the spring as shown in the link you posted. It was like a blow off valve. Once the pressure was too great, it should be able to push the filter back and bypass it. Of course, that requires a pump that is providing correct volume and pressure! ;)
     
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  11. oldolds
    Joined: Oct 18, 2010
    Posts: 3,529

    oldolds
    Member

    As you were having fuel blockage problems, I would suspect blockage in the carb.
     
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  12. Moriarity
    Joined: Apr 11, 2001
    Posts: 34,595

    Moriarity
    SUPER MODERATOR
    Staff Member

    that sectioned chevy belongs to Everett Reynolds. He is dating Darryl Starbird's daughter Christie. glad you got home ok
     
  13. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    I figured someone here would know the car. Neat to see it on the road, this time of year.

    I also caught a glimpse of what might have been the Dream Truck on a trailer going the other way, stopped somewhere. I went by too fast to see what it was.

    Thanks!
     
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  14. snoc653
    Joined: Dec 25, 2023
    Posts: 765

    snoc653
    Member
    from Iowa

    If you haven’t already found the problem, have you checked the coil and distributor advance mechanism? I’ve had the won’t pull a load problem before with those being the culprits.
     
  15. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    I suspect the distributor, but haven't had the energy to look into it yet. I got a cold a few days ago, and I'm moving slowly. Also working to get caught up with the robot the kids are building....

    One of these days!
     
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  16. Crosley
    Joined: Mar 3, 2001
    Posts: 1,119

    Crosley
    Member
    from Aridzona

    A buddy had low power problems come n go on his 1964 Econoline pickup.. He said the Condenser on the OE dizzy was bad.
     
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  17. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    Condensers usually cause rough running, or occasional missing, usually under load. Not what I'm experiencing. The condenser is the one part I replaced in the ignition system when I got the car going, I've had enough fun with them the past several years. and I brought a spare with me.
     
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  18. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    timing is slightly retarded, but not much...but there's a racket under the valve cover, and that fouled #4 plug that replacing didn't help, might have a burned valve, eh?

    compression test next, when I have a chance.

     
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  19. 1946caddy
    Joined: Dec 18, 2013
    Posts: 2,245

    1946caddy
    ALLIANCE MEMBER
    from washington

    Had a corvette that would do 100 mph on the freeway but quit going up a hill. Turned out to be plugged fuel filter.
     
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  20. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    compression test....

    compression.jpg

    and the #4 exhaust valve stem moves side to side about 1/16".

    I guess it's plumb wore out.
     
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  21. 41 GMC K-18
    Joined: Jun 27, 2019
    Posts: 4,465

    41 GMC K-18
    ALLIANCE MEMBER

    That little 6 banger gave all it had so that it could be a part of the lemons rally!
    And it got you back home safely!
    Bravo!
     
  22. Jokester
    Joined: Jan 29, 2005
    Posts: 768

    Jokester
    Member

    Looks like the head is coming off! Maybe the whole engine.
     
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  23. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    The whole engine is coming out and getting replaced anyways...but now I know how bad it is.
     
  24. Sharpone
    Joined: Jul 25, 2022
    Posts: 1,785

    Sharpone
    Member

    I know you probably posted somewhere, but how many miles on the engine/car? guessing it’s the original engine however being a taxi who knows.
    Dan
     
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  25. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    It's the original engine. The car was never used as a cab. The odometer read 88,908 when I got the car, and appears to be original mileage. There's a lot of sludge under the valve cover, could be that it didn't get as many oil changes as it should have, for a while.
     
  26. Crosley
    Joined: Mar 3, 2001
    Posts: 1,119

    Crosley
    Member
    from Aridzona

    Ya, turbo LS in the cab... then 250 inline 6 in a front engine nostagia dragster? Jim will look good in the safety gear.
     
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  27. squirrel
    Joined: Sep 23, 2004
    Posts: 58,191

    squirrel
    ALLIANCE MEMBER

    I don't really have any interest in a race-only car....
     
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  28. You did what most of acdid back in the day, drove a clapped-out engine for a great distance, lived to tell the tale.
     
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  29. AldeanFan
    Joined: Dec 12, 2014
    Posts: 1,052

    AldeanFan

    I’m not at all surprised at that wear on a taxi engine.
    Taxi cabs spend most of their lives idling waiting for customers.
    When I worked for the taxi company we had cars that would almost never get shutoff. Some cars would run back to back shifts and sit idling at the casino or airport for hours at a time.
    Cars could rack up 5000 hours without ever leaving the city.
     
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  30. RodStRace
    Joined: Dec 7, 2007
    Posts: 6,539

    RodStRace
    Member

    It was never a taxi.
    Normal wear and lack of fresh oil did it in. If you are old enough, you remember garages with Valve Jobs signs. Top end rebuilds were common back then.
     

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